Read from top down:
12/26/05 - Skip and Barbara
attended the BMRT Christmas Party at the Chatterbox Lounge.
12/25/05 - Merry Christmas
From Skip & Barbara Holbert!
I purchased 8 new exhaust valves and only needed two intake valves, which I
am waiting to come in. The heads will be ready later this coming week,
I hope.
This past week, I spent a lot of time watching TV and cleaning my office. I have so much SBC information
tucked away that I don't have room for the new library of BBC information. I
and see the need for more shelf space in my office in the
near future. I almost filled a whole garbage can with Summit and Jegs
catalogs, along with all the other mail order periodicals that are send to
me. Old computer programs that are no longer used or have been
replaced by a new version, filled a lot of garbage space. I also found
out I need to stop printing a lot of things I see on the internet. I
should make use of bookmarks and favorites to keep up with information I
want to keep, or save it to disk. Most of the stuff I printed, I never
read again, until it was time to trash it!
The engine has taken a back seat to everything, for the time being. I
will get back to it early this coming year. Holidays and "Honey Do's"
are taking a lot of my time. I think the whole world knows when I am
about to start work on the engine. That's the time when everyone can
find things for me to do.
Little Barbara got her unrestricted drivers license last week. She was 17
years old on December 11, 2005. Of course I had to take her for the driving
test. I spent a total of 8 hours, spread over two days, to get her
license. Now she wants to, and I will be happy let her, drive "Mr.
Skip"! I think I will slow the car down, maybe to around 12 -13
seconds, and let her make some passes this coming year. Hopefully, by
the end of the year, she will be ready to get her NHRA Comp. Drivers
License, then I can retire from driving. She only weighs around 120
lbs., that's worth about four-tenths off the ET, over me driving.
12/19/05 - Busy taking
measurements, after cleaning the block and spraying down everything with
WD-40. I purchased a dial bore gauge which did not come with any
instructions. I purchased a dial bore gauge to take the uncertainty
out of using snap gauges. The inexpensive ($99) dial bore gauge that I
purchased is just as hard to use as a snap gauge and micrometer. I
sent it back. I guess I have to get the $299 piece to have what I
want. I think I will pass.
My Lemons Headers arrived today!
What workmanship! They are 2-3/16", stepped, 4 into 1, with
4"
detachable collectors and evacuation fittings. They also have the temp.
bungs for dyno testing to get EGT readings. Now all I have to do is assemble
the engine, with no mistakes, put it in the body and see if they fit.
The heads are not back from the
welding repairs yet, and I still don't know how many valves I must purchase.
At this time of year, with Christmas holidays, and some of the things that
have happened in the past few months, it is hard to concentrate on building
the engine and racing.
During the past few weeks I have
been busy getting rid of junk, cleaning out my workshop and the two storage
houses where I keep my spare parts and other things. I also
inventoried all my tools and cleaned and sorted all of them. Took
everything out of my rolling tool boxes and the tool box that I take to the
track and got most of the things in good order. Mr. Van Johnson is the
inspiration for that. All of his tools and equipment are in
"Perfect Order", all the time! When I grow up, I want to be just like
Mr. Johnson :>) Anyway, now that I have everything in something close
to order, I am going to label all the drawers and try to keep the stuff like
that. My only problem is, I don't know where anything is anymore!!
12/4/05 - This may be the longest I
have ever failed to make an entry on my page. Barbara and I spent 5
days in Houston over Thanksgiving and attended the Bayou Classic. We
had a really great time. Grambling won the game, but we had fun
anyway. Barbara pulls for Grambling.
I have all of my lower end parts back. This was a very $$$$ expensive
mistake. Everything is balanced, the pistons have been notched for
more P-T-V clearance (I can use a .790 lift exhaust lift and still have
.120" clearance). I also had them relieve the sparkplugs so it is not
so critical to have them indexed just right. I found a new Comp Cams
grind that should give me an additional 40 HP over the old cam. The
lift is only .748" on the new cam, so I should have plenty of clearance.
I plan to start cleaning parts and taking measurements tomorrow. The
heads are still being worked. I saw some photos of how the welding is
coming, and it will not be long before Alvin has them back to blend in the
chambers. I hope to be ready by mid-January, when our tracks reopen.
11/8/05 -
I just purchased and received the two volume set of books on Upper and
Lower Engine Assembly from Reher-Morrison Racing Engines. What a vault
of information, especially for someone like myself that has a lot of SBC
knowledge, but very little BBC knowledge. The books cost $100
delivered, but are worth every penny. I have completed the Lower
Engine Assembly book already and have read over half to the Upper Assembly
book. I have violated so many things that they talk about in the book,
I wish I could start over with a fresh block and heads. Until I hit
the lottery, or some other windfall comes along, I will have to make do with
what I have. One of the best things I learned from the book, I hope,
is how to stop all of those oil leaks from the front and rear of the engine.
I had some bad news about my block,
two more sleeves (One of the first cautions in the Reher-Morrison book,
"Don't race a sleeved block"). I also had to have one new rod.
The rod that Eagle sent would not balance with the other seven, so it had to
be sent back. The pistons have been fly cut, spark plugs un-shrouded,
and now I can handle up to a .790" lift cam on the exhaust side and still
have .120" clearance (min. in accordance with the book). I should have lots
of clearance this time, my total lift is only .748", at this point. We
don't know what the future may bring!
The heads have not been started
yet. They had two sets of heads in front of mine, so I guess it will
be another couple of weeks before I get them back (actually got them back
on March 15, 2006), if they don't have to go
back to Dart. (For future reference, send them back to Dart.
They have the knowledge and equipment to get the job done right, quicker and
less expensive!).
I disassembled the oil pan, removed
the windage screen and the cover over the pump sump and cleaned everything.
All the screws were installed with Threadlocker Loctite. I have
purchased all my gaskets, new oil pump with welded pickup, new cam gear and
timing chain that will accept the locking tab and hex head bolts. I
cannot purchase any valves yet, they have not checked out the old ones yet.
11/2/05 - Getting back into the
swing of things, I went to check on my heads and block. Remi has just
pulled the block from the hot tank and nothing else has been done. The
heads are at Louisiana Engine Exchange and nothing has been done on them
either. I took all my push rods down there and asked them to check
them for straightness. I have asked Remi to fly cut the tops of the
pistons to give me room to use a max of a .790" lift cam in the engine.
He is also going to un-shroud the spark plugs so I don't have to worry about
getting them exactly indexed correct. Of course if the timing had not
changed, I would not have had that problem. This gives extra
insurance but slightly less compression.
I have been doing a lot of Desktop
Dyno simulations to fine the right cam for my engine. I had taken the
cam to Cam Motion to have it checked for twist and to replace the dowel pin
in the front. Everything checked out fine, and they only charged me
$15.00 for the service. This will be the least expensive thing that I
have done during this whole rebuild!
Anyway, the Desktop Dyno is telling
me that the cam I took out of the 540 is more powerful, by a few HP, that
the new, longer duration and higher lift cam that I purchased. I have
also found a few more cams that are even better, at least on the computer.
There are several areas that I can help myself. One notable area is
the headers that I have on the car, which are 2" straight tube into a
collector. If I get a set of larger diameter stepped headers, my power
curve increases dramatically, about 50 HP with the same (small, .748 lift)
cam. If I change to a slightly different, cam, I get an additional 40
HP (total 925 HP). The computer is also telling me that with the new
port and polish job, I don't have enough carb CFM.
Yesterday, 10/20/05 was my 20th Anniversary and my 67th birthday!
Barbara and I really enjoyed the day. Lots of gifts, cards and we went
out to dinner last night.
I removed the engine from the car and put it straight on the back of the
truck and took it to the Womack's Block & Head in Denham Springs, after I
had removed the pistons. Looks like another sleeve, this time in #3
cylinder and two new pistons. I had the new cam dowel pin inserted at
Cam Motion, in Baton Rouge. They also checked it for straightness.
I went over the instructions for installing the Hex-A-Just cam gear.
They recommend Loctite Threadlocker #271 and 25 ft-lbs of torque on those
three Allen head bolts. If I had followed those instructions, I would be in
good shape right now.
Marcus Bowie called and graciously offered to allow me to use his new 565
engine while mine is being repaired. I would do it, but after getting
use to all that power, I would not want to drop back to my 555. Thanks
again Marcus!
October 19, 2005 - I had lots of
help today after the timing cover was removed from the front of the engine.
Leroy Rogers, Alvin & Devin
Calhoun and Houston Hawkins were all over to analyze what happen to my
engine. The bolts in the cam
gear backed out and caused the cam to become retarded. What you cannot
see in the photos is, the dowel pin in the cam is broken off. This put the
valves in contact with the pistons and was the cause of the destruction.
The real cause of the problem was, the cam gear bolts were not torqued tight enough and I did not use the correct type threadlocking compound on the threads. I have solved the problem for
the rebuild, I ordered a 9 slot crank sprocket with non-adjustable cam gear
that I can use the regular hex bolts and locking plate for the next motor.
I suggest to anyone using the Hex-A-Just timing set that you apply Loctite
Threadlocker Red, and use a impact to tighten the Allen head bolts that come
with this set (recommended torque is 25ft-lbs). The design of the Hex-A-Just is such that you cannot
use the regular hex bolts and locking plate that I normally use on all of my
cam gears (lockwire may be a good choice for these three bolts).
October 17, 2005 - Removed left
side head to determine the extent of damage. There is a hole in #3
chamber and the head of the valve is missing. Number 7 valve head is
also missing.
See Photos
All eight exhaust valves show indication of hitting
the pistons. This would seem to point to incorrect piston-to-valve
clearance. Since I was the engine builder, there is nobody to blame
but me!
Houston came over and looked at the engine. He feels that the heads
can be fixed. It looks like I need at least two new pistons, either a
new head or repair of the busted head, eight new exhaust valves and some new
pushrods. The #7 cylinder has a scratch in the wall and may require
another sleeve (or a new block). Since none of the pistons have been
removed yet, there may be more damage that we don't see.
Alvin suggests that I check the cam degreeing before disassembly. He
thinks the adjustable timing gear may have changed and caused the loss of
P-T-V clearance.
Looks like I will be down for another extended period, since I stressed out
all of my cards to get this engine running.
I was telling Houston today, I just read on the R-M website about checking
P-T-V clearance. They do not like the clay method, that I used, or the
checking spring method, that Houston likes. I have used the clay
method, with no problem, for many years, and I had just over one-hundred
thousandths clearance on the exhaust valves.
Tomorrow morning I am taking the heads to Alvin for him to look them over.
He will determine if they can be repaired locally or if they have to be sent
back to Dart. The heads are Dart Pro-1-345's.
Anyone remember the hit song from the movie, "The Color Purple"? ("Maybe God
Is Trying To Tell You Something").
October 14, 2005 - Looks like 2005
is just not my year for racing. Back to back hurricanes and now two
engine failures in the same year. During the day Friday, I had changed
the jets in the Holley 1150 to 92/94, from 96 square after running at NPRP
Wed. night and determining that we were too rich. I changed the oil and
filter and lowered the gas pressure at the pump to 20 PSI and 8.5 PSI at the
inlet to the carb. We went to State Capitol Dragway Friday night Test and
Tune. My initial run was 9.51 @ 142 MPH making a "easy" pass.
Everything felt and sounded very good. The car came up on the
wheelie-bars, and I let up a little. It went straight as an arrow and
had a 1.380 sixty-foot time, with a 6.08 sec. eighth-mile time. We had
7.8 PSI air pressure in the M/T 14 X 32s tires. I noticed the fuel
pressure was at zero while slowing down at the end of the track. The
pressure picked back up as soon as I got on the return road. The
engine temp. on the return road was 180 degrees F. I left the line
with 140 degrees F. I came back and Houston and I pulled several plugs
to determine how everything was burning. All of the plugs we pulled
from both sides looked very good.
After cooling down and filling the
tank with VP C-14 fuel, we went back out to make an all out pass.
After driving through the water and just starting the burnout, the engine
stopped and was very hard to re-fire. This is where I should have gone back
to the pits, but like most of us would do, I got it running again and for
some unexplained reason, the line-lock would not hold to get the BO started
again (This had to be my host of Angels watching over me. I have more than
one, I get into so many things, one Angel would be stressed-out!). I
did a tire spinning burn-out up to the line and the whole sound of the
engine had changed. I staged and left the line, and I could tell the
power was down when I left. It did not get on the wheelie-bars this
time. At around the 1/8 mile I felt the same sudden loss of power that
I had experienced at NPRP on Wed. night and the engine started to miss. I
let up, and at about the 1000 foot mark I slowed and pulled over just across
the finish line. The engine was still running when I
pulled over, but very slow, maybe 3-400 RPM, and I still had oil pressure of
around 20 PSI. I got out and looked. There was a trail of water behind
the car and a puddle next to the guard rail at the side of the car (I did
not have any anti-freeze), but there was no oil. We determined that the
water was coming from the left header.
After returning to the pits,
Houston pulled #5 plug and it was wet, but when he tried to remove #3 plug,
it would not come out. Number one plug looked good, but it was also wet.
The other side plugs looked good. We carefully bumped the engine,
using the starter, and we had no compression on #5 cylinder, but we had good
compression on #1 cylinder. We put the car in the trailer and watched
the rest of the racing. "Young Blood" beat "The Mighty Carlo" for the
money in Super-Pro.
After I get the car out of the
trailer, I will pull the left side head to see what the damage is. We
will make our determination after that. I anticipate pulling the
engine, removing the pan and checking the lower end and the block. We
may have to O-ring the block to control the compression and change the
thickness of the head gaskets to provide some room inside the chambers.
October 13, 2005 - Houston woke me up this morning
wanting to know how the car ran. Two hours later he was over here at
the house helping me determine what was wrong. Glend McDonald was here
before Houston. We found a number of things wrong: The pickup for the
MSD was laying on the starter cable; some of the spark plugs were fouled to
the point of not firing; a few of the spark plugs had hit the pistons and
were not firing; the lash caps and my roller lifters are not compatible and
had to be removed (this was not true), we reset all the valve lashes. We were getting an
excessive amount of fuel into the cylinders. Michael Jackson called
and suggested we look at the fuel pressure out of the pump and into the
carb. The fuel pressure was too high at 25 psi. I normally run
around 17 psi from the pump to the regulator. The pressure into the
carb indicated 9 psi, which is what I normally run. We switched the
ignition pickup from the MSD distributor back to the crank trigger. Houston
has a good procedure for setting this device that should be a part of the
instructions, but is not available from MSD. MSD tells you how to
install it, but not how to set the timing.
I did not switch to NGK plugs, but we cleaned up
the Autolite plugs and used them. We also switched back to the Holley
1150 CFM carb. We also rejetted the carb to lean it out some. I
had changed two of the plugs and had not bothered to index them. When
we started the engine, it sounded much better than it did earlier, but still
not as good as I wanted. We pulled the two plugs that I had put in
earlier and they had both been hit by the pistons. These two plugs
were the only ones that were not indexed. We indexed those two plugs
and everything sounds excellent! The engine is very crisp and
responsive. We have decided to put index washers on all 8 plugs to
give them a little room in the combustion chamber. I will change the
oil tomorrow from the brake-in oil, Quaker State 30HD, to Havoline 10W-40
Synthetic.
I hope to go to State Capitol Dragway tomorrow
night to try to get some seat time. When I ran at NPRP, I had not
driven in so long, that I forgot where my line-loc switch was to do my
burn-out. I did have a .004 green light on my first pass! Some
things you never forget!
First time out since April 30, 2005
October 12, 2005 - Went to NPRP
today. The results were not good. Something is not letting the
engine rev up above about 5500 rpm without losing power. I made two
passes and each time the car sputtered and acted up just after leaving the
line. The engine did not sound good in the burnout either, and it
wants to die as it comes out of the burnout and at the end of the track.
On the way home from the track, I
decided I will remove the new sparkplugs and go back to my old NGK-8 plugs.
I have used these plugs for about 7-8 years with great success. The
last time I tried to switch to another brand, I seem to remember having the
same problem that I am having now. Houston has experienced this same
type problem and traced it to the plugs. At the time, we were both using the
same brand plug.
While at the track, I removed 7 of
8 plugs and 5 of them appear to be very rich while two, # 5 and #8,
appear to be lean. I cannot check #7 plug without taking the steering
apart. I have jetted the carb rich, on purpose, for this testing
session. I even changed back to my old standby, BG-1090 carb.
The timing was checked at 35 degrees and everything else seems to be OK.
Tomorrow I will do a leak-down check and compression check (which I
never did, this would have helped locate the problem). I put 5
gal of VP C-16 gas in the tank just before this testing session. That should
have taken care of any detonation.
October 11, 2005 - The UPS man
showed up with my seal kit for the BG 400 Fuel pump. Let me say that
the seal kit for the 280 pump and the 400 pump are not the same.
Sonny, a Pro-Fab, had a 280 seal kit that I could have used, but the large
O-Ring is not the same size.
I have installed the seal and
tested the pump. Everything works very well and there are no leaks
from the fuel pump. The car is finally off the jack stands for the
first time since May of this year. I should be able to make it to NPRP for
Weds. night test and tune. I will make tow or three easy passes.
I want to take it to Pro-Fab either Thurs. or Fri. to have the alignment and
corner weights checked. Then I want to take it to State Capitol
Dragway Friday night. We hope to make it to the Battle on the Bayou on
Sat. at Louisiana Raceway. This is a very aggressive schedule, but FUN!
October 9, 2005
- Washed and polished the car today. I had some Eagle Aluminum Wheel
Polish in a small black bottle that I used for the first time on my aluminum
wheels. This stuff is awesome! I normally use Mother's, but I
was out, and did not feel like going to the store. I have no idea
where I got the bottle of Eagle polish, but it works great. The wheels
had not been done since around Mardi Gras time early this year and were in
bad shape. I did all four wheels, by hand, in about an hour.
I removed the
fuel pump to get ready to overhaul it. There are 5 bolts on the bottom
of a BG 400, and one of them takes a special tool to remove it. I went
to Lowe's and Sear's, but no luck. The head of the bolt has three
vertical slots, spaced about 120 degrees apart, and the top of the bolt is
tapered. I tried everything that I could think of, with no luck.
Then I came up with the idea of using a small Die, from a tap & die set, to
remove the bolt. Some of the smaller dies have three cutters in the
center spaced 120 degrees apart . The larger dies have four cutters.
The three prongs of the die are a perfect fit and I was able to remove the
bolt with no harm being done to it at all. I also mounted my
transmission cooler to the front of the radiator and installed the K&N
Filter Charger on the Holley 1150 carb. The BG and Holley have
different center hole heights, so a special cut all-thread rod had to be cut
to put the filter on the Holley (actually what comes with the filter will
fit a Holley out of the box. I had modified that to fit a BG Demon
carb).
Oct. 8, 2005 -
Houston got on the phone and found a BG 400 Repair Kit at Product
Engineering in Long Beach, California. We ordered the kit and it
should be here on Tuesday. I will remove the fuel pump and get ready
to install the seals. I am continuing to work on stopping the last oil
leak from the back of the pan. I have a lot of cleaning to do on the
car, the rims, and the inside, to get back to looking the way I want it.
The car could stand a paint job, but I have to recover from rebuilding the
engine before that can happen.
I may be able to
get to the track on Weds. evening for some test and tune at No Problem
Raceway Park. That would give me time to fix anything I find before
this coming weekend, Oct. 15th, for
"The Battle On The Bayou"
at
Louisiana
Raceway
. They also have a regular bracket race on Sunday at
Louisiana Raceway.
October 7, 2005 - I tried real hard to make it
to the track, but failed. The first order of business was to check the
trans fluid after warming up the engine. I also checked for leaks into
the water system while the engine was running. I purchased 4 belts,
each one-half inch different, for the alternator and had to modify the
alignment, after Glend pointed out that the alternator was not straight.
I installed one of the belts and tested the alternator. Reggie and
Glend helped me bleed the brakes. I changed the oil and filter.
I captured some of the oil to be sent to a testing lab for analysis. I
had three significant oil leaks on the front, rear and passenger side of the
oil pan. Using "The Right Stuff" sealant, I stopped two of the leaks and
reduced the rear leak to a drop about every 2 hours. I should be
able to totally stop that leak with another application of the sealant.
The back-breaker was a fuel pump leak. The leak was from the
junction of the pump and the motor on my BG 400 Fuel Pump. Another
component that did not like the long layoff. We took everything apart
and reassembled it, only to have the leak get worse. We gave up on
trying to go to the track. I still have some things that I need to do,
but the fuel leak is the big problem now. I will have a new or rebuilt fuel pump
by Wed. of this coming week.
October 6, 2005 - Completed the check list
and started the engine. Something is wrong! It was very hard to start
and then ran as though it was really retarded. Changed the timing on
the crank trigger IAW the instructions and ran out of room to advance the
timing using the crank trigger.
(3/23/06 - The real problem was the cam bolts were loose and allowed the cam
to go to full retard.)
Reconnected to the distributor and got
the timing set on 34 degrees, but it still will not respond correct.
Very unresponsive and hard to idle. Frustration has set in and I am
quitting until tomorrow. I will inspect the springs and set the valves
again.
Later:
After sitting and thinking what the problem could be, I changed the
distributor cap. I had installed one with a large hole in the top so
that I could phase the rotor. This helped a little, but not much.
Me being a carburetor man, I just knew it could not be the carb, but I
changed it anyway. That was the problem! I must have done
something wrong when I overhauled my BG 1090 during the long layoff.
Anyway, the engine sounds very good with a Holley 1150 CFM Dominator on it.
Not as strong as I had thought, but we will have to see what it does on the
track. With any luck, I should be testing at State Capitol Dragway
tomorrow!
Much Later
10/6/05: I warmed the engine and reset all the valves. Checked the
timing at 35 degrees. This perked it up a bit. Still not as
strong as I thought it would be. The oil pressure is 60 PSI at 160 degrees.
That is as high as the temp would get after 20 min of running at 2000 RPM.
Tomorrow I will change the oil. I have two oil leaks. One from
the front of the engine and one from the rear. I hope they seal
themselves, but you know that never happens. I will have to try to
seal them, somehow. The transmission is not leaking at all.
My alternator
project is becoming a real headache. The mounting bracket for the
radiator is too close to the hot terminal of the alternator. I had to
cut a notch in the radiator bracket. I also had to purchase two,
longer screws for the alternator to align the pulleys. The next thing
is to trial fit belts to make it work. This will be an adventure to
figure out what length belt to use.
October 5, 2005
- Spent most of the day connecting everything. I had to remove the
transmission pan and put a new gasket on the pan, along with sealant on the
threads of all the pan bolts to stop some small leaks. I charged the
batteries and cleaned all the connections. The starter is installed
and the headers are in place on the left hand side. Because I
installed the disk brakes while the engine was out, the header on the
drivers side interferes with the brake line for that wheel. I had to
move the line and wrap it with heat shield bandage to protect it.
I have a long
check list with about 20 items to be done. I should be ready to start
the engine sometime after Noon tomorrow.
October 4, 2005
- While I had the pan off, which has no provision for a dip stick or a sight
glass, I poured in 7 qts of oil to see where that would come in relation to
where the crank is spinning. That will get the oil almost to the
bottom of the crank. Next time the pan is off, I will get a plug
installed at that level so I can tell where the oil level is.
555 CID BBC ready to be installed.

Rolled the
engine out of the workshop and dropped it into "Mr Skip".

October 3, 2005
- I won't be taking the car to Pro-Fab on Weds. When I dropped the
distributor to line it up, I noticed the oil pump shaft was hard to turn.
The steel sleeve on the shaft that connects the oil pump to the bottom of
the distributor was binding. I removed the pan and found the pin in
that sleeve was out of the two little holes. I cleaned everything up,
purchased a new ARP steel shaft and put the pan back on. I also gapped
(.045") and indexed all the plugs.
October 1, 2005 - The past few
weeks have been very stressful to all of us. Tomorrow I have people coming
in to stay with us as a staging point while they go down to New Orleans to
survey their property and get belongings. The city has twice as many people
as we had in the past and the traffic, always congested, is now twice as
bad. I purchased trailer insurance Friday from my State Farm agent for my
enclosed trailer. It will cost $60 every 6 months. I think that is a good
deal. I purchased 10 gal of racing fuel Thursday for $77.50 (a
bargain).
State Capitol Dragway is also
experiencing a resurgence. With No Problem Raceway Park closed until
mid-October, there are many cars at the SCD weekly Friday races. Last night
was a packed house. If you are coming to race at SCD, please bring your own
gas. They may not have any at the track. Bracket Masters Racing Team would
like to sponsor a Sat. race at State Capitol. We have to convince Ronnie
that having a Sat. race will be good for the track. We will continue to try
to get him to see things our way and allow us to have the race. We would
like to do it in early 2006, maybe in Feb. or March.
During the past few days I have
worked on my engine to get it ready to go back into the car. I checked all
of the rocker studs and torqued them to 50 ft-lbs. The stud girdle was
installed and the valve covers and intake was installed. We mounted the
water pump with the front motor plate, installed the electric motor for the
water pump and put the crank trigger in place.
I had my old single wire alternator
checked out by P&R Alternator and Starter Repair.
These guys do good quality work and they have rebuilt my two mini-starters
in the past with great success. I had to fabricate a mounting bracket that
puts the alternator on the frame of the car. It is adjustable and will face
the engine on the drivers side and be driven off a pulley on the damper in
front of the crank trigger wheel.
I have a few
small jobs to complete before installing the engine. After I get the engine
installed, I will measure for a new set of headers. After I get them, I
will let everyone know what they are and how I like them. I made an
appointment with Sonny at Pro-Fab to get the front end aligned and to have
the car scaled on Wed. of this coming week. I expect to test this coming
Friday night at State Capitol Dragway to get ready for the Battle on the
Bayou at Louisiana Raceway.

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