Read from top down:
3rd Quarter 2006 Racing
6/29/06 - How is it possible to be
so happy one moment, and be completely upset the next? We went back to
finish the dyno session this morning. I put fresh oil into the engine.
When we tried to spin it, it stopped. We thought the carb had leaked
down and filled another cylinder, as it had done yesterday. Not this
time! Number 3 cylinder was full of water! Everything else was
dry. We pulled the head and could not see the source of the water.
The cylinder walls looked good and the head did not have visible cracks.
Number 3 piston did not look like the others when it came to the amount of
deposits on top of the piston and on the head too. Lane Whittington
called the machine shop and told them to get ready to pressure test a
cylinder head. We took the head off and took it to be tested.
The results of the test were, both the intake and exhaust valve seats were
leaking where the new seats were installed into the head. Apparently,
the machine shop that did the work (not Tim's or Womack's), tested the heads before installing the
seats. After installing the seats, they went into the water jacket and
a leak under both seats was the result. The head is on its way back to
Dart for repairs, which is what I said I should have done in the first
place.
If I had bypassed the dyno testing,
this would have happened anyway, most likely at the wrong time, and I would
be replacing more parts. Plus I would have had the engine in the car
and I might have been in the final round of eliminations! I can't wait
to see what my 1/8 mile times are when we put it back together. It
should be just in time for those 1/8 mile races at NPRP this Summer.
6/28/06 - Wonderful experience!
Today we started our dyno testing at
Tim's Engines in Denham Springs, LA.
The dyno crew consisted of Lane Whittington, Jason Reppond, Chuck, of
"What's Up Chuck Racing" and Tim Whittington.
The engine is awesome! Before
lunch, we warmed up the engine and made three low RPM pulls. The first
pull to 5000 RPM, netted 702 HP and 738 ft-lbs torque, and the curve was
going straight up. At 5500 RPM, the HP was 755 and the top torque was
745 ft.-lbs. and the last pull before lunch, we went to 6500 RPM and netted
817 HP with top torque of 748 ft.-lbs. The engine timing was set at 36
degrees and we had the Holley 1150 carb, with 92/94 jets installed. We
were using VP C-14 racing fuel. We pulled two plugs and they were very
light. We decided to richen up the carb.
We got ready to reset the valves
and Lane saw a very small amount of metal flakes in the top of the head
where the oil drains back to the pan. After consulting with several
people, including engine assembly people from the machine shop, we decided
to put a screen in the top of the oil filter and we changed the
filter. I told them about the installation of the heli-coil on the #3
intake valve, with the head installed on the engine, last week. This
engine also has a total of 4 sleeves. The last two were installed in
#3 and #5 cylinders. This may be the source of some of the metal
flakes. After
lunch, we reset the valves to the recommended .026" intake and .028" exhaust
(all of the exhaust valves required resetting. They were all too loose.
We changed the rotor cap and installed one with a hole in it so we could
check the rotor phasing. We warmed up the engine again and let it run at about 2300 RPM for about 3-5 mins. to allow the oil to circulate. We pulled the filter and
inspected the screen. There was almost no metal present. All of
the experienced engine builders agreed that we could continue with our
testing. The rotor phase was right on target at #1 pole in the distributor
cap.
We decided to make a pull up to
6800 RPM, and we got up to 821 HP with top torque of 743 ft-lbs. At
the end of the day, we had made 13 pulls, none higher than 6800 RPM,
changing carbs, changing timing and changing jets in carbs. The
highest numbers were achieved using the BG King Demon carb. The BG did
not have the floats set and the Idle mixture was not correct. It also
leaked down and filled a the heads with gas. When we ran it, the jets
were at .094" square and timing set at 38
degrees. The HP was 841, with torque of 763 ft-lbs. This was 5 HP
higher than any run with the Holley. The worst pull was
at 34 degrees timing (down from 36 degrees) and jets at .098 square, with
the Holley 1150 CFM carb. The HP also fell off when we went from
.094/.096 jets up to .098 square with the Holley carb. We reinstalled
the Holley carb after two pulls with the King Demon. We will work on
the BG carb and get it corrected. We drained the oil, which looked
very good, and went home. We will continue in the morning. I
want to make at least a couple of more pulls with the K&N Filter Charger in
place. I also want to put the BG back on and try to correct its
problems.
By comparison, my DynoSim computer
dyno predicted 867 HP with top torque of 745 ft.-lbs. That is fairly
close to the 841 HP & 763 ft-lbs on the real thing.
Afterthought: The computer
dyno (at home) could not do the break-in runs, or find any problems that
exist within the engine. In the time of about 8 hours, we have found
out more about the engine than many hours and runs at the track would have
taken. Now I have a basis for the information that my computer program
tells me. I can now make changes, using the computer program, and see
what the effect SHOULD be. I think it is time and money well spent to
have the engine dyno tested.
6/24/06 - It's Done!!! Ready
to go to the dyno this coming week. Check back on Friday for the
results. Today I put the stud girdle on and reset all valve lashes
after tightening the stud girdle. Some of then moved and had to be
individually reset (#3 intake moved about .002" and had to be reset.
Some of the others moved more than that). The valve covers are on, the
intake is bolted down and I put the crank trigger device on the front of the
damper and dropped the distributor. I put in 6 1/2 qts of standard
10W-30 oil in the pan and the filter took just over 1/2 qt. The final
assembly is very tight. Takes a lot to turn it over. The spring
pressure is very high on these new springs.
6/22/06
6/23/06
6/24/06
6/23/06 - Bright and early this
morning I went to the industrial Screw and Fastener Co. and picked up enough
heli-coils to do the whole head. I only used one. Alvin and I
talked it over and decided to fix only the stud holes that would not torque
to 55 ft.-lbs. The fix was not without its own adventure. After
installing the new threads and installing the stud, when I put the rocker
and adjusting nut on, I noticed the rocker roller was not sitting in the
correct location. A quick measurement using a straight edge across the
4 studs, indicated the repaired unit to be off center by a few degrees.
This was the result of using a hand drill to make the pilot hole for the tap
and not getting the alignment perfect. I thought about a lot of
different ways to fix it, including taking it to a machine shop, but in the
end I put a shim under the push rod guide plate and then installed the stud
and torqued it. I had to do this three times to get the correct size
shim. The torque on the #3 intake rocker stud is 65 ft.-lbs., while
all the others are 55 ft.-lbs.
When I started to set the valve
lash on the first set of valves after setting #3 intake and exhaust, as I
turned the crank I heard a loud "Crack"! I stopped turning and started
to look for the source of the noise. Number #3 intake push rod guide
plate, where I had put the shim, had broken. The crack was just
outside of the area where the new heli-coil was installed. I rechecked
the alignment of the 4 intake studs, and they were still in perfect
alignment and I did not see anything else wrong. I checked the torque
on the stud and decided to leave it. Since I run a stud girdle that
clamps around the tops of each rocker stud adjusting nut, I don't think too
much bad can happen if any of the rest of them pull the threads out. I
would let a machine shop install any other heli-coils that need to be done.
I completed setting all the valves,
installing all the lash caps and checking the torque on all the intake and
exhaust valve rocker studs. The cam calls for .026" intake lash and
.028" exhaust lash. For this "cold" setting, I took .002" off of each
setting. After the engine is hot, I will reset the lash to the correct
setting.
6/22/06 - After laying off working
on my engine for so long, there is a tendency to forget things (especially
at my age). I
installed the odd side head, torqued it down and put the rocker arms on.
I had set 3 of the 4 sets of valves on that side before I thought about the
lash caps! While loosening #1 intake to put the lash cap in place, the
whole thing started to turn, stud and all. Now that lets me know that
I should have torqued all of the rocker studs before I put the rocker arms
on (I ran into this same thing the last time I did this in August last year
[I need to put this step on a checklist. Is that right Mr. Johnson?]). When I tried to torque #3 intake, it would not tighten. I
was trying to go to 55 ft-lbs torque. The
threads were bad. The Reher-Morrison book says to put heli-coils in
all of them. The exhaust studs seem to be much longer than the intake
studs because the intake studs reach into the intake passage on the Dart Pro
1 heads that I have. I don't know enough about BBC heads to know if
this is the same in all BBC heads, or just my Dart Pro 1's. I wonder what else is wrong with these heads?
I am going to check ALL of the rocker studs and put heli-coils on the ones
that will not reach 55 Ft-lbs, or that feel like they may give out. I
will purchase enough to do all of them and I may just do all the short ones
(intakes).
I called to make an appointment to
have the engine dyno tested today. After careful consideration, I have
decided to go to Tim's Engines for my testing. Layne and Tim
Whittington have been a loyal supporters of Bracket Masters Racing
Team during the past few years and they have a very nice, new dyno testing
facility.
June
18, 2006 - Skip participated in the Father's Day race by working on the
gate and taking photos during the day.
6/11/06 - Remember to get your
state inspections on your cars, trucks and trailers. That's right, in
Louisiana, your trailer is required to be inspected each year, just like
your car and trucks. Because trailers and Diesels don't require the
emissions test, the inspection only costs $10.00 for trailers and diesel
engine vehicles. There is no insurance requirement on the trailer.
I got mine done this weekend.
6/6/06 - The hood looks good!
Perfect match, which is exactly what Mr. Allen (the painter) said it would
be when he looked at the paint. To get the perfect match, I took the
trunk over to B & T Paint and they used an electronic color matching machine
to get the correct mix for the paint directly off the trunk. I am
really happy with the way it came out. I had a lot of running around
to do today and have not been able to devote the time to get everything back
on the car to see how it looks with everything in place. At first
glance, it looks very good. It even passed Barbara's critical
inspection (which almost never happens!).
Today I talked to Attorney Robert
Randolph, who is also a racer. He started out with, "He's Back!"
I was shocked, and flattered. He continued by telling me how he
follows my progress (or lack of) these last few months and how much he
enjoys reading about my engine work. He said he missed reading about
the car while I was on vacation. I really enjoyed talking to him.
Most of the time when I write this
stuff, it is so I will have a record of what I did and to make sure I can
retrace my steps, especially if I screw up something. It is also very
helpful to be able to go back and capture an old combination that worked. I
know many of you out there reading about my work on the car can see when I
do something stupid, but I hope that when you stop laughing, you learn
something from my mistakes. On the other hand, you may learn a few
good things too.
I was informed yesterday, by my
church, that I have been selected to teach the Youth and Young Adults
in Vacation Bible School this coming week. That will put a severe
crimp in the time I have to work on the car. If it will help save one
kid, it will be worth it. This will be my 4th year of teaching in VBS.
June 5, 2006 - Returned from
vacation yesterday. I
left the hood to be painted before I left for vacation. I will pick it
up tomorrow. It will match the front end of the car and will not have
stripes.
Now that the vacation is out of the
way, I have some other pressing family items to complete early this coming
week, but after that I plan to make an all out attempt to get the engine
dyno tested as quickly as possible.
May 19, 2006 - I finished the new
cowl induction hood. Now
all that is needed is the paint. I have contacted a man about doing the
hood in the near future.
The more I cut off, the lighter it
became (dah...). The final configuration is actually a little lighter
than the old one, but is more flexible. I think it needs reinforcement
across the back opening, and I think I can invert a small strip that I cut
out and contact cement it into the top inside of the scoop.
With the 8" engine set-back in this
car, I should be able to take better advantage of the high pressure at the
base of the windshield. No more black plugs!
I think I will tackle the Lexan
windows next. The car has all of the original glass, with the roll-up
mechanisms. The exception is the two small rear quarter windows, which are
already Lexan.
I had a complete set of letters,
numbers and decals, made for the car, truck and the trailer a week or two
ago. I am going to have the hood painted solid purple, and remove the
stripes from the rear and paint the back quarter panels solid purple.
Then I will apply some new, different, stripes along with new rear quarter
decals.
May 17, 2006 - The hood is almost
complete. The 8 Dzus fittings are in place and they all line up and
work! Thanks to Mr. Van Johnson! Now all I have to do is cut the
back part of the cowl induction to allow the air to get under the hood.
I went over to Eddie Fisher's home and made a template off of the old
"Masterpiece". Now I can cut the new hood to match the old one.
One exception, the old one was 4", and this new one is 6" tall. I
moved the oil and gas gauges over exactly 3 inches to fit under the opening
in the hood.
The Inaugural William "Dub" Lewis Fathers Day Race, Quick-8, will
be sponsored by Popeye's and will pay $1000 to the winner. The
quickest Quick-8 car, under 7.00 seconds, will get an additional $250.
I watched Ronnie "FoFo" Ferret play
with his beautiful blue and white Corvette last night at State Capitol
Raceway, on a rare Tuesday night Test & Tune. The engine, a 632 CID
BBC, needs a little more fuel to reach its potential. Last night he
was testing a 1350 CFM carb. The current 160 GPH fuel pump is not near
enough to feed this monster all the way down the track. Ronnie has a new 500
GPH fuel pump on order. I can't wait to see the results. There
was another beautiful car out there last night, a candy apple deep red Vega.
I spoke with the driver and found out the car has a 383 SBC under the hood.
The car ran some very respectable very low nine-second runs. The car
sounds awesome, a very, very strong 383...
May 16, 2005 - What a night last
night on TV. I had two VCR's going and still didn't get to see or tape
all of the shows I wanted to see. The President screwed up all of my
start and end times for my VCR settings, tapes ran out or stopped short of
the end of the show, it was a mess. I had choir practice, so I didn't
get to see Prison Break, thank God for Blogs, at least I could read about
it. Two and One-Half Men, Old Christine and the two-hour Gray's
Anatomy final show, back to back with the continuation of CSI Miami.
Just too much for one night. I should purchase one of those new DVR
units, but even if you record them, when do you have time to watch?
Yesterday, during the day, I worked
on fitting up the new cowl induction hood. What a mess! Most
people that have seen my car know I have my fuel and water temp.
(correction, oil) gauges
mounted outside in the line of sight of the driver. These have to be
relocated to install the new hood. I also had to cut off approximately
7 inches from the rear end of the hood. Van Johnson came by and
instructed me on how to make a template to fit the hood to the existing cowl
panel where the gauges are mounted. The last thing that I must do is
the most critical. The Dzus fittings have to be installed. This
hood is not as light as I had hoped for. In fact, it may be the same
or a little heavier than the old one. I still believe the air flow
will be much better. Only time and experience will tell.
Does anyone own a 12 point, 1/4"
socket? I have many sets of 3/8" drive and 1/4" drive sockets, but
until I went to Sears (Lowe's doesn't sell them loose), I did not own one.
I was using those 12 point bolts on the two bolt holes that clamp the front
of the oil pan to the timing cover. I changed them out to Allan head
screws. Much easier to deal with, even though I bought the sockets.
I want to have everything ready for
the Father's Day Shootout at State Capitol Raceway on June 18th. They
are going to have a Quick-8 Doorslammer bracket. I would love to get
one of those 8 spots. I have missed all of the other events that I
wanted to make this year, maybe I can make this one. I can already
think of 8 -10 cars that run quicker than what "I think" my car will run
when I do get it out there. Even if I don't run quick enough to get
into the Q-8, I can still run in Super-Pro. It should be a fun day.
Father's get to do what they want
too on Father's Day, without feeling guilty! I do hope all of you
treated your Mom's and wives that are mother's to a nice Mother's Day...
Do you know that some women without children are some of the best mother's
in the world.
Next time you go to State Capitol
Raceway, take time and visit the VIP lounge in the tower on the 2nd floor.
Remember the open room with nothing in it that was there for the past few
years? Now it has wood floors, a flat panel big screen TV with a big
sofa to watch the shows, they also have two other big leather sofas in front
of the two picture windows for the VIP's to sit and watch the races.
The walls are paneled and they have things on the walls. The lighting
is even real nice. If the rest of the proposed improvements to the
track are going to be as nice as the tower (the office downstairs is laid
out nice too), we are going to have a first class track in Baton Rouge.
The Friday night crowd has returned and the racers like the new management.
Congratulations to Owner, Mr. Lanny Lewis and Track Manager, Gary Carter.
May 8, 2006 - While sleeping (this
happens to me a lot), I had a dream about the drive train of the car.
Seems everything was working well, except the Torque Converter was missing!
I could not find the torque converter anywhere and in my dream, I could not
get the car to leave the line. I woke up and early Monday morning, I
called Custom Built Torque Converters in New Orleans to, first of all, see
if they were still in business after Katrina, then to find out if they could
freshen up my torque converter. The man said "Bring it on!" They
are still in the same place in Marrero, LA off the West Bank Expressway.
I found the converter in my work shop, covered up and ready to be
reinstalled. Remember, I have just had the transmission overhauled at
TCI. I looked at my old records and thought I had had the torque
converter freshened up the last time I had the tranny reworked. That
was in 2004, and I only had around 140 runs on the units. When I got
to Custom Built, they looked and said the overhaul date was March of 2002!
That converter must have over 300 runs since Custom Built freshened it the
last time. This was originally a BTE 9", 4500 stall converter, built
to go behind the 540 BBC engine. At 200 runs, I had had it freshened
by Custom Built. At the time, it was working just fine, but when they
looked inside, it had worn Torrington bearings and some bushings were worn.
They checked everything and they welded the fins in place.
I did not ask for this fin welding and thought it may effect the stall of
the converter. I was assured it was only to strengthen the converter.
When I put it back in and ran it, I could not tell the difference.
From what I am told, once the fins are welded, you cannot adjust the stall
again, without replacing the part that was welded.
Fast Fwd. to May 2006. They cut the converter open and everything on
the top looked good, including the Torrington bearings and the stator under
the bearings. When he removed the stator (may not be the correct name
for that part), underneath it, on the stationary part where the welding of
the fins was done, was a broken fin, just laying over and still connected at
the top, where it was welded. Had it not been welded back in 2002 we
were looking at a disaster. Thinking about what may have happened if I had
chose not to have it freshened up this time, it could have been lights out
for the new transmission. We will never know how long it would have
lasted, but other fins may have been ready to break off too. I had
noticed about 200 RPM change (higher) in finish line RPM during the last few
full passes that I had before the engine failure last April 05. I had a rear
end failure back then too, and I thought the RPM change may have had
something to do with that.
Custom Built is going to check everything inside and replace what is
necessary. It will be ready Weds. and I will go get it Thursday.
The cost? Only $175.00! Willie says that is cheaper than
insurance.
Willie Beathley and Van Johnson had both been telling me to get my converter
freshened up. My wife Barbara even offered to help pay for the converter to
be done when I took the tranny to TCI. The lady at the receiving dock at TCI
even questioned me about my converter. Everyone was warning me, but it
took a dream to make me move. Maybe that was GOD tapping me on the
shoulder and telling me to listen to my friends.
Due to faulty record keeping on my part, I had convinced myself that the
converter only had 140 runs, it was working well and did not need to be
freshened. I have learned my lesson. When the tranny comes out
for overhaul, the torque converter will be done at the same time.
April 28 - May 4, 2006 - During the
past few days, I have participated in the Glen Oaks High School Car Show,
the Career Day at Prescott Middle School (I took the Jr. Dragster to both of
these) and I went to the Sr. Breakfast for the graduating seniors at Glen
Oaks High School. Little Barbara is graduating this year and we are so
proud of her. The Baton Rouge SMART Program has awarded two $750
scholarships to students that completed the Glen Oaks Auto Tech Program.
I had the pleasure of presenting the awards to the students at the Sr.
Breakfast. Little Barbara was awarded a certificate for being the best
student in her Computer Science class, and she passed her Microsoft Computer
Certification test a day later.
April 19, 2006 - Worked on a lot of
little things that are important. Put the new bronze gear on the
distributor. Installed the new window net. Installed the new
seat belts and fixed the parachute handle. I need a new parachute
cable. Cleaned up the room where I
work on carburetors and stored tools.
I came across an interesting bit of
information while reading my Upper Engine Assembly book, by Reher-Morrison
Racing Engines. Gaps on spark plugs should be between .030"-.035" on
racing BBC engines. For years, I have used .040"-.045" spark plug gap.
Today I reset my 8 new Autolite plugs to .032" gap. The Autolite' s are also
new for me, I have used NGK in the past.
April 13, 2006 - Still have not
done anything to the engine. Been real busy doing my taxes. I
plan to have the car ready for the Glen Oaks High School Car Show for 2006.
The show will take place on April 28, 2006. Racers are invited to
bring their cars to the front lawn of GOHS at 9:00 am until Noon for the
show. The show gets bigger each year and the kids really enjoy it.
The car show is free!
April 11, 2006 - Picked up my head
from Womack's Block and Head, where Rick had resurfaced the head. He
took off .005" to clean up the scratch. He said it was deeper than we
thought and it was a good move to have it resurfaced.
April 7, 2006 - After thinking long
and hard, I've decided to remove the head with the scratch between #1 & #3
cylinders. I will take it to a machine shop to get the surface cleaned
up again. When we did the cc of the chambers, we had
approximately123.8 cc on one of the reworked chambers and 123.3 on the other
one. The other two are also just over 122 cc. I can have .005"
taken off the surface of the head and only reduce the chamber volume by 1
cc. The scratch may not be that deep. The other head has volume
between 121.5 cc and 122 cc, so I will be real close to even on both sides.
I think this will be better than taking a chance, especially when the
scratch is right under the gasket. The additional down time will be
worth it.
Late Afternoon - 4/7/06 - The
machine shop looked at the scratch and said it was not something (deep
enough) that I should worry about. He did say, if it was his, he would
resurface it, especially since it was right under the head gasket seal
between the cylinders. I will have it done and I should have the head
back on Monday. They said approximately a .003" cut would clean it up.
State Capitol Raceway is having
their first Sat. Bracket Race under the new management, on Sat. April 8,
2006. Everyone is super elated about the new changes and we are all
looking forward to some great Saturday racing.
Bracket Masters Racing Team
normally has a family picnic at State Capitol each year. We will be
looking for a Saturday bracket race to have this event.
3rd Quarter 2006 Racing
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